Hi all.
I am face to face with next problem.
I am using TMS320F28375D chip and and can_loopback_interrupts example for CAN module.
Its test Interrupts loopback and TX pin of harware.
I set up bit timings to achive 1mbs for CAN, see good CAn message in TX pin by oscilloscope.
Loopback working with out errors
But if puts controller to normal states without test bit no TX activity on pin. But interrupt driving work fine with out error.
Any idia?